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Posted

I wouldn't have a clue. I never took note, of all the times i've pulled the ʞ©$ɟer out. Has red around the outer part. Can't see much more than that.

Posted

Stereo is all finished plus a fire extinguisher. Got an accelerator pedal now too! Clean windows, carpet and car. Still need an alternator. Are they esay enough to rebush yourself?

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Posted

This car looks grouse Gavin. :y:

 

That's no good about the RWC. Just whip the blocks out and sort out the chassis with a Welder. :yes:

 

Josh :cool:

Posted (edited)

Thanks for the kind words mate! Not sure how i'm going to handle this just yet. The lowering blocks staying for now. But the chassis has been organised for next week.

 

The dude was an uber tight arse. Had a winge about the structural work that had been done before I got the car. Had a winge about my home made exaust, The little pod thing on the rocker cover that "should run to the air cleaner". It is a ʞ©$ɟing air cleaner!

 

Didn't like the 5k because its not a standard replacement engine or equivelant replacement. Apparently if I put the 4k back in, with which it was originally registered with, it would still need to be engineered.

 

It's a good thing he didn't charge me.

Edited by GJM85
  • 3 weeks later...
Posted (edited)

Just did a little tune up and took it for a blat round the street. Man its noice to drive. Just pulls along nicely from a stand still too about 4 grand. The tacho stops working there so I don't give it anymore. Either need to source a MSD tach adapter or lose it all together. Half my street is a real steep hill but in 3rd gear, not a problem.

 

I found the standard valve clearances of .20mm & .25mm as recommended in the gregories manual is a bit slack and noisey.

.12mm & .15mm sounds perfect.

 

The plugs appear to be perfect. So i'm very happy with the a/f mixture. 125 pri & 162 sec, 79 idle.

 

Timings at a neat 10 degrees. I'm a little concerned about the Streetfire Ignition. I might take it out and try the electronic dizzy again. But I do like the old 3k dizzy.

 

It's not really about perfomance anymore. It's about the drive and a part from the home made exaust, its a ʞ©$ɟin nice 'n' easy one.

Edited by GJM85
  • 1 month later...
Posted

It's been a while. Not much has happened. I'm kind of sick of seeing this thing sitting in the garage gathering dust.

I took the streetfire box thing out today. No sense in it being there. Had to reset the timing and idle speed.

 

Doesn't run much different, maybe better, other than the flat spot between gear changes. Could be the exaust leak. Pops like crazy on over run. I've got another brake switch because the last one I got ʞ©$ɟed out rather quickly and I lost my brake lights. That little ʞ©$ɟer is harder to change than the starter motor.

 

Anyway no plans to get this thing on the road yet. I'm poorer than a snail without a shell.

  • 2 weeks later...
Posted (edited)

Brother got this on Friday. 91' Cressida Grande.

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Other brother got this today. 86' 4 Runner Turbo Diesel.

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Combined they spent 3400$. Jealous? Yes! :yes:

 

But I still got this...

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Edited by GJM85
  • 3 weeks later...
Posted (edited)

Today I decided to take the sidedrafts off and see what the go it. I hate the lack of room around that damn manifold, as it took me over an hour to get the carbies and the manifold undone with my big fumbling mits. Once they were off I held them level and twisted open the throttle to see how much fuel they were squirting. Cylinder 1 - moderate, 2 - heaps, 3 - nothing, 4 - nothing.... no wonder it was running like dogs balls on chop day.

 

Had this problem today with my 5K, pulled the fuel line fittings off and found a heap of rust had come through the fuel filter and was blocking the screen on the fitting on top of my solex's.

Edited by Crostek

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